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Detailed Engineering Design Services for EPC of CPSF Debottlenecking and Capacity Upgrade at Turkmenistan

Client

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Contractor

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Duration

August 2022
-
February 2024

Central Processing and Storage Facility (CPSF) handles production from LAM and ZHD fields

Capacity: 100,000 bpd oil, 25,000 bpd water, 200 MMSCFD gas

The debottlenecking study and capacity upgrade studied issues in liquid & vapor streams and to upgrade for future production and increased water handling

Scope of Work (SOW):

  • Reroute liquid outlet from slug catcher

  • Retrofit LP three-phase separator

  • Install new equipment (Water Bath Heaters, Oil/Water Transfer Pumps, De-sander Cyclones, Gas Scrubber, Flow Transmitters/Control, Substation Building, Battery Room, FACP, UPS, Instrument Air Package)

  • Expand control & monitoring systems

  • Upgrade firefighting and F&G detection/protection systems

  • Install associated piping, valves, control systems, safety systems, fittings, strainers, sample points, analyzers

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